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I'm using FreeJoy to build an FCCB joystick based on the TM Warthog, and I ran into a problem. I have two axies connected to the MCP3202, and they work fine when the CD4021 isn't involved. But as soon as I plug in the TM Hornet, all the axis outputs go wrong—the zero points are wrong, and bring a lot of signal jitter. I’m guessing the two chips might need different CLK inputs, but I’m not sure. Any advice on how to fix this would be really appreciated. Thanks a lot!

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